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#1 | |
Rotary Fanatic
Join Date: Feb 2008
Posts: 302
Rep Power: 18 ![]() |
Quote:
Maxed out the NPR intercooler ![]() We turned it up to 22 psi and had some blow out issues. Then came crank case issues, then some run funny issues which resulted me quitting ![]() I think I have a side seal thats sticking or floating. At idle the vacume is at 16 inches which is normal. from 3500-4500 it has a sputter like something is messed up. After that it is crisp and clean. ![]() |
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#2 |
Rotary Fanatic
Join Date: Feb 2008
Posts: 302
Rep Power: 18 ![]() |
This is the sheet before I quit. It had a rich misfire and the crank case was making a huge mess. Since there was only a minute gain, I figured it wasn't worth going any further... My 20 psi curve is very nice and not chopped up like these we were having a problem with.
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#3 | |
600rwhp club member.
Join Date: Mar 2008
Posts: 551
Rep Power: 18 ![]() |
Quote:
Congrats.. 475 is plenty to make that car go fast! |
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#4 |
Rotary Fanatic
Join Date: Feb 2008
Posts: 302
Rep Power: 18 ![]() |
That intake manifold changed peak TQ from 5800 to 6800 RPM. I don't know what the car is going to do, but the car is 60 WHP stronger 7500-8300 which is about what I wanted at the same boost level. Since there is 4.88's in the rear, I wanted to bump the limiter up instead of running a lower gear set.
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