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Needing a new tow rig.
Join Date: Mar 2008
Location: AR
Posts: 245
Rep Power: 18 ![]() |
and here it is installed. This is where i found the coolant drain plug loose! damnit the only 2 things i didnt check came back to bite me in the ass. Once it was tightened and my tool installed ops check GOOD.
![]() once again on to finish breakin mileage. at this point it was about 6-7 hundred into it so time to give it more RPM to 6k and a couple pounds of boost 3-5max. This is where i started having problems with the sequential system. So long story short i believe i had every single seq boost problem on the forums and still couldnt get it t work right. I mean i checked everything replaced some solenoids re route vac lines so on and so forth. Now i planned on going single later anyway so... out with all the seq for poor man non-seq. hurray much simpler works as advertised. This was at about 850-9 mileage and i was sick of working on it and wanted boost and it to work. in my book my break in was done at that point so once i made a HOME DEPOT manual boost controller to mantain 10 PSI i was in it to win it! >>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>>> >>>>>>>>>>>>>>>><<<<<<<<<<<<<<<<<<<<<<<<<<<<<<<<<< <<<<<<<<<<<<<<<<<<<<<<<<<<<<<<<<< up to this point it has all been to make my newly aquired FD run in a stock fashion. Now its on to start making it MY OWN performing road car. TRANS BRACE: First things first i was missing the 3rd gear shift as for some reason the trans tail shaft was flexing quit a bit. So the fix I decided to use was a transmision brace that i made being i had the material and ability. once installed it made a WORLD of difference in drivability, especially running an ACT solid 6-puck. EXHAUST: Of course i wanted to do an exhaust as i was still running a stock cat and some redneck catback. I then decided to do a 4" setup although i knew it would be loud i did not know how loud. i picked up some 4" bends and started running it from the 3" twins downpipe by necking it up to a 4" v-band. then ran it back to a magnaflow 4" oval race muffler to a single 4"inlet dual 3" outlet flowmaster super 50 hd. Reason being i still wanted a slightly covert twin exit at the rear yet still be able to flow. at this time i picked up a banzia/pineapple rear diff brace(the one that will clear a 4" pipe) and installed it being i was there already. TWINS: Now that i had a rather free flowing exhaust i was experiencing boost creap as the stock wastegate was not flowing enough. I removed and disassembled then to port the wastegate unfortunatly my air compressor istoo small to run my die grinder so i ended up doing it with a dremmel. i dont have any pics of it but i opened it up to the outer edges of the flapper door and it know maintains boost perfectly with the large exhaust. Last edited by proz07; 02-21-2009 at 08:30 PM. |
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