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07-31-2016, 07:45 PM | #1 |
IT'S ALIVE!
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My '79 Log Thread
Got my SA running correctly and picture-worthy so I figured it's time to start a thread. Some may recall the for sale thread but I purchased this 1979 from a gentleman in Nebraska and had it shipped to me in Virginia. According to the VIN this is S/N 2944 and it was built in March 1978. It currently has ~26,400 miles on it.
Overall, I'd rank the car an 8/10. There are a couple scratches and dings and there's some discoloration on the hood where it appears something was spilled on it. There's minimal rust underneath. The interior is immaculate aside from some loose carpet in the hatch area. Hopefully with a little work I'll get this back up to a 9/10. The plan is to keep this completely stock and hold onto it for a long time. I'll update this thread as I work on the car. |
07-31-2016, 07:50 PM | #2 |
IT'S ALIVE!
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What I've done so far (7/31/16):
-Fixed the driver's side window (popped out of its channel) -Titled and registered in VA -Charged the battery -Replaced the alternator -Replaced the steering column top bushing -Washed the exterior -Changed the engine oil and oil filter -Flushed the brake fluid The last record I have of the brake fluid being changed was from 1988. If that's true it's no surprise the fluid looked like this: Should be more of a pale, American lager color and not a brown ale, no? A new fuel filter, Redline MT-90, Redline 75W90, OEM thermostat, and spark plugs have been ordered and I've got 3 gal of 50/50 coolant sitting in the garage. I'm basically completely the car's 25,000 mile maintenance at this point. |
08-01-2016, 07:12 AM | #3 |
Waffles - hmmm good
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Nice SA! About time some folks on this site show a little 1st gen love! Those waffles still
look new. I would replace the master/slave soon. Probably a lot of corrosion in there. Do the hose too at that time. How does the brake fluid look? You should probably start collecting all the rubber hoses to replace the stock ones. At this age they are all probably deteriorated.
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1980 GS stockport, Fat Nikki, RB Dual Facetfuel pumps, Holley regulator, RB Street port exhaust, 2GDFIS, MR2 MK I electric fans, 2G strut bar, relayed fans, lights and fuel pump, LEDs Project Fat Nikki Budget 12A rebuild Video setup < $30.00 |
08-01-2016, 09:49 AM | #4 | ||
IT'S ALIVE!
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08-01-2016, 01:29 PM | #5 | |
Lifetime Rotorhead
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08-01-2016, 07:26 PM | #6 |
Waffles - hmmm good
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Rebuilding seems like a good idea on the MC/WC/Calipers until you have to redo em 6 months
later. Trust me I know. Right now I have a leaking right front caliper because a) I couldn't get a rebuild or new one on the right side and b) I went ahead amd rebuilt it. It works ok until it decides to spew fluid at some point under hard braking which then elicits load squeeling until it burns off the leaked fluid. I definitely wont track it like that and will have to either rebuild or replace with a good unit. I must have pinched the piston seal somewhere during reassembly.
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1980 GS stockport, Fat Nikki, RB Dual Facetfuel pumps, Holley regulator, RB Street port exhaust, 2GDFIS, MR2 MK I electric fans, 2G strut bar, relayed fans, lights and fuel pump, LEDs Project Fat Nikki Budget 12A rebuild Video setup < $30.00 |
08-02-2016, 12:16 PM | #8 | ||
IT'S ALIVE!
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08-12-2016, 08:36 AM | #9 |
IT'S ALIVE!
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Changed the oil in the differential and transmission as well as replaced the fuel filter.
Changed the spark plugs and decided to check the timing and condition of the distributor. I adjusted the points gap but the rotor and cap have seen better days so I decided to order new parts. Replaced the rear window struts so it'll stay up and not come crashing down on my head at random times. Still need to flush and fill the coolant at some point and I'll be replacing the thermostat at the same time. This'll be it for the general maintenance for a bit. I'll enjoy the car for a few more months this year and get it set up for the Winter. Next year I'll probably replace all the suspension and steering bushings and maybe attempt to rebuild the carburetor. |
08-22-2016, 12:19 PM | #10 |
IT'S ALIVE!
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Overhauled the distributor: new points, rotor, cap, and 3 of the 4 condensers (I mis-read the Parts List), and replaced the spark plug wires. Got the timing set, which was a bit of a chore. The leading timing was easy but I can't seem to get a good signal for the trailing timing. I set it as best I could then went about adjusting the idle fuel mixture and idle speed per some guidelines I found online. The car seems to be running marginally better. Every now and then the tachometer "bounces" a couple hundred RPM at idle/low engine load. I opened the points gap up closer to .020 in. and that seems to have helped but it still happens. Crappy aftermarket points? Who knows.
Snapped a couple pictures of the dirty interior: Once I finish the maintenance I'll go back and detail the car. Trying to get it ready for the Fall car show season. |
08-23-2016, 06:10 AM | #11 | |
Lifetime Rotorhead
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If this is what is going on, you can try moving the pickup/wires around to try to increase the distance between the pick-up and any leading wires. This helped me, but I didn't have consistent luck with it on my GSL-SE, so being an EE, I modified my cheapo timing light to adjust the pickup's sensitivity. What I did was put a 5K ohm variable resistor (linear taper) in series with the pick up lead. To use it on the trailing wire, start with the variable resistor set at 0 resistance (max sensitivity), and dial it back until the timing light stops flashing completely. Then SLOWLY dial it back up (add resistance) until the light just begins to flash again. If you didn't overshoot, you should now be seeing consistent flashes only on the trailing signal. |
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08-23-2016, 07:08 AM | #12 | |
IT'S ALIVE!
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12-01-2016, 10:31 AM | #13 |
IT'S ALIVE!
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So just to bump this after a while. I drive the car 10 miles or so a week. I think I've put like 150 miles on it since I got it. Since the last update I've completed all the basic tune-up maintenance. Back in late August I swapped in a new-ish OEM midpipe (the one between the thermal reactor and heat exchanger) since the old one had rusted through in a couple places.
The tachometer bouncing at idle is getting slowly worse. I've since swapped the original OEM distributor parts except the points back in with no noticeable impact. I'll try them next. I noticed the bouncing will stop with even the slightest throttle input. For example, the throttle up response from turning on the A/C will cause the bouncing to stop. I've read claims ranging from bad connections/grounds, to bad alternators and igniters being the cause. It doesn't sound like the car is missing at idle so I'm thinking it's more of a signal issue. Another question: does everyone's SA smell bad? Like excess exhaust emissions bad? I've adjusted the idle mixture and speed per recommendations I found online and while the idle itself has improved the car still smells like it's running with zero emissions equipment. I also noticed the throw out bearing is kind of noisy. It's not squealing but I have a decent, low-pitched whirling noise when the clutch is engaged (pedal out). 5th gear also has a pretty good whine to it that's load/speed dependent. I'll probably do a clutch job next year and when the transmission's out I may pull the tail housing to look at the 5th/reverse assembly. |
12-01-2016, 04:01 PM | #14 |
Waffles - hmmm good
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You don't like that smell? My wife hates it but shes a girl. I suspect the TR is
not doing anything for emissions anymore because I bet a number of issues with the carb plumbing may be causing it. Also the SAs do weird things with the trailing firing (or not firing depending on gear you are in and a couple of other factors). This is all controlled by that little box the ignitors live in on the fender well (its a 79 so maybe no ignitors). Anyway, the idle being lumpy like that may be a timing issue or a mixture issue when no advance is being applied. At idle the vacuum should be zero and no advance happens. As soon as you give it gas it will advance pretty quickly. Go through the ignition section of the FSM and make sure its all set to spec if you haven't already.
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1980 GS stockport, Fat Nikki, RB Dual Facetfuel pumps, Holley regulator, RB Street port exhaust, 2GDFIS, MR2 MK I electric fans, 2G strut bar, relayed fans, lights and fuel pump, LEDs Project Fat Nikki Budget 12A rebuild Video setup < $30.00 |
12-02-2016, 01:59 AM | #15 | |
Temporarily insane.
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Posting simply to get the updates of this car. Beautiful and it seems to be in good hands.
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For my collection of short stories: Kindle Nook |
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