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RX-7 2nd Gen Specific (1986-92) RX-7 1986-92 Discussion including performance modifications and technical support sections. |
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04-06-2009, 10:45 PM | #1 |
Test Whore - Admin
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Oil Pump O-ring Mof - Testers NEEDED
So here's the backstory, my last engine was a 13B-RE Cosmo motor with the stock oil pump, stock OPR, stock bypass valve and stock casting under the pump itself. At idle I would see about 15ish psi and on decel the low psi warning light would come on @ 15 psi I believe. I've seen as low as 7psi and the most I ever saw with that motor, I checked the logs, was 67 psi @ 6k+rpm. Not great but "acceptable." I use that term loosely. The pump, when I broke the motor apart was visibly scored.
The engine needed a rebuild and I wanted to really address the oil system for a myriad of reasons. I decided to go with 1) FD OPR 2) Shim the bypass with 2 washers 3) Clean up the casting under the pump 4) MAKE A POSITIVE SEAL BETWEEN THE ALUMINUM PUMP AND THE IRON MOUNTING SURFACE. A friend of mine has a CNC mill and when I approached him about the idea, he kinda scoffed at it saying that no-one has ever done it to his knowledge and people don't seem to have problems so why bother? It didn't take long for me to convince him to try it and I sent him a stripped down and cleaned up pump. It was actually the one that was visibly scarred. There was no scaring on the pump body, just the troicoids and the pieces between them. I had a second pump on it's way to me anyway. This is what we have. I cleaned up the casting, nothing crazy, about 20 minutes of work And here is the pump body And here is the o-ring installed with a smear of hylomar on the seam between the o-ring and the outside sealing surface to keep the o-ring in place and on the mating surface itself. THe hylomar cannot get into the pump. Also of worthy note is my dual mocal oil coolers run in series with -10 line. Theres close to 15' of -10 line which should also reduce the pressure some. bulkhead fittings T-Stat The results, well the are RIDICULOUS. At a fast cold idle I'm seeing close to SEVENTY psi. (I'm going to type out the numbers so you know it's not a typo) At a normal hot idle I'm seeing thirty-five psi and by Two-thousand eight hundred rpm's I'm seeing over a hundred and nine psi. I have the standard 0-100psi 0-5v sender and it's pegged at 109. I don't know what my max psi is yet becuase I just don't have a sender that reads that high. One is on order. Right now my dash is throwing a "code" and readin 0.0psi which obviously causes me concern. Upon first start-up when the rpms climbed high enough the dash read 0, it's default error. I quickly shut the motor off. It took me a minute to realize what was going on. I had to open up the Motec and bring up a dial gauge that read the voltage from the sensor. With the voltage pegged I realized what was going on. I called my aluminum chip eating friend to tell him and he was pretty surprised. However, we are not sure how much of it is the o-ring, and how much of it is the motor itself, the builder, the tolerances I used, the FD OPR, etc etc etc. It's all me, the builder Anywho, what we are looking for are people that are rebuilding motors that aren't going to change ANYTHING else in thier oiling system. We can't use my experience as an example becuase I did so much at once we cannot be sure what mod effected the pressure. For all we know the o-ring did nothing and it was the change in pump internals and the FD OPR. I doubt it. My gut is telling me that the o-ring made a significant difference but with so many variables, we cannot be sure. I have however done some research in both the FSM and with other peoples experience and it looks like my pressures are MUCH higher than other peoples with similar mods. I should also mention that the pump was actually worn PAST the FSM specs as measured with the feeler gauge. I didn't have a third pump on hand so I played musical internals until I got the closet tolerances I could. They were still out of spec though. In otherwords, the pump should've been thrown out but instead, it's making more pressure that the FSM states as minimums. In most instances, 2x the amount. Is there anyone that wants to actually test this mod? The o-rings came in packs of 10 so you'll be getting a free o-ring. The machining we are not sure of the cost. He seems to think there won't be any interest. I told him I thought he could make a decent coin offering this service if we can prove that it significantly raises oil pressure. The first testers would pay very little if anything for the machining. It's up to him, not me. But if we could get a group of people that wanted it, I'm sure the cost would be insignificant. So, if there's anyone who wants to try this - post up, or PM me. I'll be putting this thread in every relevant section just so it can get attention. However, if all responses can be placed in the "General Rotary Engine Related Tech Section," that would be great. Thanks guys |