View Full Version : My 38K mile 93 SSM build
fire85gslse
11-23-2008, 05:26 PM
Ok guys and gals, a lot time planning for this day and it has finally come. I have owned the car for a bit over a year now. Bought it with 36K on it and well really have not driven it due to this work not being done.
My stock 93 SSM with 38k stock miles getting some work to make her last longer. Keep in mind I am not looking for HP but more dependable good power.
Once complete here is what will be done and staying Sequential. I will be trying to take pics of everything done and will be posting them.
So first to come....... my car in stock trim currently with:
SSR rims
Front cross drilled rotors
Petit AST - coming off going AST delete
New Poly motor mounts
Stainless Steel Brake lines
Eibach springs
99 Spec rear lamps
RB single tip cat back
Xcessive alum oil pan - Coming off going back to stock
fire85gslse
11-23-2008, 05:35 PM
Whats to come:
AST removal
Alum Radiator
Turbos ported and worked to keep my sequential
rats nest to be thinned out
coils relocated
cerma coated UIM, LIM with block offs
wiring harness to be thinned out and cleaned up
some water ports to be tapped off instead of just blocking them
TB to be worked a little
Garfinkle Motor works torque brace
Garfinkle Motor works oil pan brace
SR Motor sports SMIC
Greddy piping and elbow
1300 cc injectors
Efini cross over pipe
greddy boost controller
Power FC with commander
Wide band
down pipe
mid pipe
Beck/Arnley clutch kit
ETC............
alot of cleaning and small work that will be posted
need RX7
11-23-2008, 05:37 PM
Dang, 38k miles? Very nice. I like what you've got planned too. :icon_tup:
fire85gslse
11-23-2008, 05:45 PM
ok here are some beginning pics:
Motor getting ready for removal.
Note the second pic on the driver side frame rail from where the battery sits.hard to get to area to keep clean. Well I will have to clean that up before the motor goes back in.
fire85gslse
11-23-2008, 05:53 PM
pictures of motor out and the frame rails painted in a black bed liner coating to help with rust/scratches. There was a seem that I followed to keep it uniform on both sides.
Time to replace every water hose under the hood (those that I will be keeping) all gaskets, studs/nuts on turbos and some other small odds and ends. Ray at Mazda sent me a box of goodies for almost $700 needed to do this work.
fire85gslse
11-23-2008, 06:04 PM
Here are some before pictures once the turbos were pulled off. See all the cracks and where the gasket sits. Now to basically gasket match the turbos and that will help with some cracks. The others will have to be welded.
Whizbang
11-23-2008, 06:13 PM
great condition car!
fire85gslse
11-23-2008, 06:39 PM
Turbo worked performed by Garfinkle Motor Works (Thanks David)
You can see the cracks have been welded, some grinding has been done, and see the black spots in the flat surfaces (low spots due to warping). Those will be resurfaced to get some/most of that taken out.
Here are those pics
fire85gslse
11-23-2008, 06:58 PM
more on turbo work (Garfinkle Motor works)
fire85gslse
11-23-2008, 07:08 PM
more pictures of turbo work done by Garfinkle Motor works
fire85gslse
11-23-2008, 07:16 PM
pics
fire85gslse
11-23-2008, 07:19 PM
My cheap Radiator that I had to modify the shroud to fit. Had to use bolts and nuts to mount it on the bottom and had to open up the holes on the shroud top sine it all was not lining up perfect.
Then I had to notch the shroud since the upper tube was at a different angle over the stock location (seen in the next group of pics).
If you buy one of these keep in mind that its not a direct drop in nor does it have a drain or a line for the AST.
If I would had known about this up front I would have spent more for the right one.
But again $150 for this was not too bad even with the mods I had to do.
fire85gslse
11-23-2008, 07:35 PM
more radiator pics.
Had to remove the name on it
fire85gslse
11-23-2008, 07:45 PM
Here is my motor sitting there now with the turbos back on.
Chadwick
11-23-2008, 09:15 PM
See you decided to pull the motor. Makes the work you are doing a lot easier. David is the turbo porting master. Work looks great.
Dan
fire85gslse
11-23-2008, 09:18 PM
See you decided to pull the motor. Makes the work you are doing a lot easier. David is the turbo porting master. Work looks great.
Dan
yep pulled it the next day after talking with you. Will go back in complete and ready.
Brent
11-23-2008, 11:47 PM
Looks great so far Chad! Can't wait to see it all finished up!
Terrh
11-29-2008, 04:21 PM
hey, I think we had a bit of a chat at deal's gap!
I was with the canadians, had the skyline GTR.
Thanks for the link to the WG porting, hopefully I'll be taking my FD to the gap next spring.
fire85gslse
12-02-2008, 01:07 PM
more motor pics as she is coming along
rx7 vinnie
12-03-2008, 09:22 PM
I want your unmolested car soooooo bad.
Garfinkles Motor Works
12-11-2008, 09:37 AM
A new rats nest has been made with four valves ,Chad will post pics of it soon .
fire85gslse
01-08-2009, 12:15 AM
Well fuel system is done, new rats nest built, oil pan brace on, and motor ready to go in this weekend.
therighthand
02-07-2009, 02:27 AM
Any plans to produce the hard lines for the solenoids?
Chadwick
02-07-2009, 07:47 AM
Any plans to produce the hard lines for the solenoids?
Yes, contact Garfinkle to have your rack modified. Well worth the price!
Dan
fire85gslse
02-15-2009, 11:29 AM
Got my 99 Spec y-pipe back and man it is slick looking
fire85gslse
02-15-2009, 11:36 AM
Also garfinkle completed this thing...... cant remember what it is called but it sure did clean up and loose a few tubes that were not being used anymore
fire85gslse
02-15-2009, 11:48 AM
This picture is where the Master Polisher David gave me a few pointers on how to polish, so I sand blasted 3 parts and started to polish one...... not complete but not bad looking for my first time. It was cool to see the part coming to life.
Did not think it took that long to work one part nor that much sanding to make it look good.
Last two pictures is that of the tube that goes to the rear turbo. Garfinkle polished it (cleaned up a little) and some of the unwanted mounts were cut off and sanded out. Became a clean slick looking part! Sorry but I was excited to get it on the car or I would have taken pics before I mounted it.
Got my 99 Spec y-pipe back and man did garfinkle make it slick looking by cutting off the Blow off valve nipple in the middle, welding in a plate and working it to flow with the lines. Then polished it out to make it a work or art. Im going to attempt to polish the upper tube myself so i can get an understanding on the labor it takes and time that is involved in one part.
What BOV will you be using and where will it mount?
fire85gslse
02-15-2009, 01:28 PM
What BOV will you be using and where will it mount?
HKS on my elbow as well as my air temp.
fire85gslse
03-28-2009, 09:49 PM
Sorry for no new pics, my build has hit a slump, and time is killing me right now. I will have to bring it back home in a week or two finished or not. Lets hope time is my friend these next two weeks.
More pics to come as it moves on. There are alot of mods from Garfinkle Motorworks that have been done that I need to post. He reinforced my sway bar mounts and they are built like a tank now. Man did Mazda fail on that mount!
Brent
03-29-2009, 11:35 AM
The stock sway bar mounts are horrible!!!! Mine were bent and cracked when I switched them out with my widefoot ones?
fire85gslse
04-15-2009, 07:41 AM
The stock sway bar mounts are horrible!!!! Mine were bent and cracked when I switched them out with my widefoot ones?
Yes, they are weak from the factory.
fire85gslse
05-13-2010, 09:09 PM
wow, has time gone by.
Well just to update everyone I got back on the car 3 days ago. Had everything back on and ready to load it up to take it to get tuned.
Well sad story is that it tried to catch on fire - fuel circuit / wiring issue somewhere. Now to let the pros figure that out and fix it for me.
Hope to be back up running soon................
Max777
05-16-2010, 04:03 PM
Wow, this is impressive! I like the neatness of your build, and how you invested money in all the right components. Also, that turbo work must have cost you a kidney, right? I didn't even know it was possible to weld those turbos back up and machine them like that.
fire85gslse
07-25-2010, 07:23 PM
Update:
Took the car to Tweak It Racing in Symrna to have it finished.
Dan and Brian have put alot of time into this car and have found the following issues wrong with her.
1.They found that the car had the o rings missing on the injectors and filled the motor up with fuel. Thats fixed....
2.They found the wiring that tried to catch my car on fire. New coil harness, coils relocated back to the OEM spot and thats fixed......
3. Now the turbos are shot. Primary is not boosting and secondary is blowing smoke from sitting in gas for 3 months.
Hope soon to have the issues worked out and car back on the road.
luke6813
07-26-2010, 01:25 PM
Man I hate that for you. I was wondering what was going on with this build. Your car only had 38k on clock right? How did all this happen. Its good you moved your coils back to the stock location. Your mounting location was right next to your steering rack, which is about the worst place you could have put them. Besides you never hear of the FD having a problem burning out coils with the stock set up. I think someone was just trying to sell you something.
How did your turbos go out so quick? Your car is mostly stock right? Unless you run high boost the stock turbos are almost always good for 80 to 100k. I know hind sight is 20/20 but i think your biggest mistake was going that deep into a prestine FD to begin with. That and not having someone with you who is knowledgeable about FDs to help you out.
Well I hope you get it all sorted out and start enjoying your 7 again.
fire85gslse
07-26-2010, 09:38 PM
Man I hate that for you. I was wondering what was going on with this build. Your car only had 38k on clock right? How did all this happen. Its good you moved your coils back to the stock location. Your mounting location was right next to your steering rack, which is about the worst place you could have put them. Besides you never hear of the FD having a problem burning out coils with the stock set up. I think someone was just trying to sell you something.
How did your turbos go out so quick? Your car is mostly stock right? Unless you run high boost the stock turbos are almost always good for 80 to 100k. I know hind sight is 20/20 but i think your biggest mistake was going that deep into a prestine FD to begin with. That and not having someone with you who is knowledgeable about FDs to help you out.
Well I hope you get it all sorted out and start enjoying your 7 again.
miles 38K miles stock. As for the coils, it had plenty of clearance from the rack and that was the least of my concerns. It was being under the FPR and the wire going to the TII coil done wrong that I was concerned with.
Turbos were soaked in fuel for 2-3 months as the injector O-rings were missing which filled up the turbos and motor with gas.
It was not a mistake to go into the car, the mistake was not just taking care of my true concern and just enjoying the car.
As for not having some one with me, well I actually did but thats neither here nor there now.
fire85gslse
08-14-2010, 12:13 PM
ok, a few lessons learned!
What not to do!!!!!
1. Dont move the coils to the frame rail. Why not you ask? Well FD coils typically dont go out. Not only that but it was a directly under my FPR if it should have ever leaked fuel.
Now if you dont have these issues or concerns then go ahead.
2. Dont upgrade to a T2 coil unless your very careful when splicing the wire.
Mine was upgraded and the person who did the wiring grabbed a small shielding wire and crimped it into the hot lead. Over a short time it melted the wires and shorted them out within seconds of causing an engine fire. I was lucky that it was in the drive way with hood up or I woul dhave never seen the black/green smoke.
3. Dont run the stock belt on a air pump delete kit. It allows the pulley on the kit to barely rub the flexible intake tube causing a hole. make sure to go down to a smaller size.
Over the last 2-3 months I have had to redo all the vacuum lines back to stock to try and trouble shoot all the small issues which should be fixed. Once I get a good set of turbos (looking into rebuilds) on the car I will hopefully be back up and running.
I would be lost with out all the help of Dan and Brian at Tweak It Racing in Smyrna. They have found everything listed above, corrected it and have the car closer to being back on the road soon. Thanks Tweak It guys!!!!!!!!
ok, a few lessons learned!
What not to do!!!!!
1. Dont move the coils to the frame rail. Why not you ask? Well FD coils typically dont go out. Not only that but it was a directly under my FPR if it should have ever leaked fuel.
Now if you dont have these issues or concerns then go ahead.
2. Dont upgrade to a T2 coil unless your very careful when splicing the wire.
Mine was upgraded and the person who did the wiring grabbed a small shielding wire and crimped it into the hot lead. Over a short time it melted the wires and shorted them out within seconds of causing an engine fire. I was lucky that it was in the drive way with hood up or I woul dhave never seen the black/green smoke.
3. Dont run the stock belt on a air pump delete kit. It allows the pulley on the kit to barely rub the flexible intake tube causing a hole. make sure to go down to a smaller size.
Over the last 2-3 months I have had to redo all the vacuum lines back to stock to try and trouble shoot all the small issues which should be fixed. Once I get a good set of turbos (looking into rebuilds) on the car I will hopefully be back up and running.
I would be lost with out all the help of Dan and Brian at Tweak It Racing in Smyrna. They have found everything listed above, corrected it and have the car closer to being back on the road soon. Thanks Tweak It guys!!!!!!!!
What happened to your turbos that Garfinkle ported?
fire85gslse
08-16-2010, 05:28 PM
Don, its posted back a few post.
When the motor was put back in the injectors did not get the O-rings somehow.
Brought it back home and turned the key on to roll up the window. Well the Turbos filled up with fuel the couple of times I had to turn the key on and sat in it for 2-3 months. Also there were a few pluming issues with the turbo system that Tweak It had to track down over top of the wiring that tried to catch fire. To be honest, way too many issues that were overlooked in the begining some how and I just hope I can get it back on the road. Right now the cars faith is in the good hands of the guys at Tweak-It racing (Dan and Brian) who I owe alot!
diabolical1
08-16-2010, 07:12 PM
oh boy, what a saga.
glad it "tried" to catch fire as opposed to actually catching fire ... would be sort of ironic given your screen name and all.
in all seriousness though, i'm glad you caught all the issues at this stage - before catastrophe - and it seems to be a matter of time before you'll have it on the road again. good luck, Bro.
fire85gslse
08-16-2010, 08:31 PM
oh boy, what a saga.
glad it "tried" to catch fire as opposed to actually catching fire ... would be sort of ironic given your screen name and all.
in all seriousness though, i'm glad you caught all the issues at this stage - before catastrophe - and it seems to be a matter of time before you'll have it on the road again. good luck, Bro.
wow, have not heard from you in a long time..... since the old carb deal we did way back.
Yes the lack of fire was truly only minutes away and with the car only having 38K miles I would have cried like a big baby. Being a firefighter it's not good to have our own stuff catch fire. Kinda looks suspicious.
diabolical1
08-16-2010, 10:14 PM
yeah, it's been a while since we were in touch. :) i'm glad to see things working out for you. hey, since your turbos were just sitting there when they went bad, they should be rebuildable, no? i mean it should just be a matter of new seals and such, right?
duval7
08-17-2010, 06:15 PM
So it was Garfinkle's modified ignition harness that made your car catch on fire. I have a feeling thats how he burnt my FD down too.:banghead: Its a tragedy that he has such a good reputation on here and people who actually know him would never let him come near there car. I learned this the hard way.
fire85gslse
08-21-2010, 01:21 PM
yeah, it's been a while since we were in touch. :) i'm glad to see things working out for you. hey, since your turbos were just sitting there when they went bad, they should be rebuildable, no? i mean it should just be a matter of new seals and such, right?
From what I have been told no but now I have a few sets that I hope to use to get one good set built. Looking at BNR's website he can basically pull the inners out and replace.
So it was Garfinkle's modified ignition harness that made your car catch on fire. I have a feeling thats how he burnt my FD down too.:banghead: Its a tragedy that he has such a good reputation on here and people who actually know him would never let him come near there car. I learned this the hard way.
It was the coil harness due to the shielding wire was crimped in with the power wire. Ended up melting and shorted out all of them. After dissecting the harness and looking at each wire it was plain as day.
I would not recommend any moving or swapping to a T2 coil to anyone. Its not worth the chance of a fire and really after talking with several fd builders they say fd coils dont really go out.
Herblenny
08-21-2010, 02:16 PM
I would not recommend any moving or swapping to a T2 coil to anyone. Its not worth the chance of a fire and really after talking with several fd builders they say fd coils dont really go out.
yeah, I've always told people not to swap to T2 coils.. but there are few that insist T2's are better. I've had no issues with stock FD coils and will never replace them.
GorillaRE
08-26-2010, 12:22 AM
So it was Garfinkle's modified ignition harness that made your car catch on fire. I have a feeling thats how he burnt my FD down too.:banghead: Its a tragedy that he has such a good reputation on here and people who actually know him would never let him come near there car. I learned this the hard way.
Did you read ANY of the things this guy wrote? His car had so so many things wrong with his whole damn setup... But no, "DAVID" caused it. Use your brain, show some respect and get a life.
-J
duval7
08-26-2010, 01:27 PM
Did you read ANY of the things this guy wrote? His car had so so many things wrong with his whole damn setup... But no, "DAVID" caused it. Use your brain, show some respect and get a life.
-J
Yea "this guy" lives about half a mile from me and I have helped him out alot with his car. His car was pristine when he bought it with absolutely nothing wrong with it. Before you go bashing what i said why don't you talk to some Tennessee people about David. There is a reason people have stopped taking there cars to him, thats why we call it being GARFINKLED.
djmtsu
08-26-2010, 01:34 PM
Everything that was wrong with it happened while it was in David's possession. From what I am told.
So he is within his rights to call him out.
sbrian2
08-26-2010, 03:39 PM
:lurk5:
fire85gslse
10-26-2010, 05:56 PM
well got some new turbo's, getting it tuned and hope to have to back soon.
cant wait...... been too long and too much extra money
fire85gslse
12-23-2010, 10:38 PM
Turbo's on, car is tuned with spring pressure (7psi) right now and made almost 300 at the rear. Should be interesting once the boost is up and car is tweaked.
Im enjoying Putting miles on her. About the crack 40K and that will be a day I might cry....... She has been in the 30's for a long time and for a 93 to have under 40K it is clean and what I have wanted since I first saw it in 93.
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